超级13Cr抗CO2腐蚀油管热轧缺陷原因分析与控制

    Analysis and Control of Cause for Defect of Super 13Cr Anti-CO2 Corrosion Oil Tubing as Occurred during Hot-rolling Process

    • 摘要: 简要介绍了超级13Cr油管的开发背景、生产工艺流程及主要技术指标;通过理化检验和金相分析,探讨了超级13Cr油管穿孔、热轧典型缺陷形成的主要原因,并提出改进措施;介绍了工艺改进后超级13Cr油管的实物质量水平及现场应用情况。分析认为:δ铁素体的存在是造成超级13Cr油管表面出现热轧缺陷的主要原因;通过合理设计超级13Cr钢种的化学成分,严格控制坯料加热温度,可有效控制δ铁素体的产生。

       

      Abstract: Briefed in the paper are the development background, the manufacturing process flow and the main technical specifications of the super 13Cr oil tubing.The main causes for the typical defects of the said tubing as occurred during piercing and hot-rolling processes are investigated via related physical inspection and chemical analysis as well as metallographic analysis.Accordingly, relevant improvement measures are proposed and taken. Also elaborated here are the physical quality level and the feedback from the field operation of the super 13Cr oil tubing as produced with the improved manufacturing process.The analysis identifies that the existance of ferrite δ is the main cause for the said defect.Therefore ferrite δ will be effectively controlled via actions as proper design of the chemical composition of the 13Cr steel, and strict control of the billet heating temperature.

       

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