T91毛管穿孔工艺的研究

    Study on Piercing Process for T91 Steel Pipe

    • 摘要: 针对热轧穿孔T91管坯生产过程中产生的顶头耗损严重,毛管内折和毛管端部外表面裂纹等问题,通过采取重新制定合理的加热参数、调整穿孔参数和改进工模具,有效解决了穿孔顶头损耗大,毛管内、外表面质量波动较大的问题,使顶头的小时穿孔支数达到125支,平均每个顶头的穿孔支数达到400支左右,大大提高了生产效率,成本下降显著。

       

      Abstract: There exist certain problems during the hot-piercing operation for the T91 pipe,including high plug consumption,and occurrence of inner fold and end-outer surface crack of the shell,etc. Accordingly,proper heating parameters and piercing adjustment parameters are determined,while relevant operational tools and dies are modified. As a result,the above mentioned problems concerning high plug consumption and obvious inconsistency of both outer and inner surface quality of the shell are solved,which leads to such a efficiency that the productivity of each individual plug is up to 125 pieces per hour,and the average productivity is about 400 pieces,resulting in considerable enhancement of both the shift output and the cost effectiveness.

       

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